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Ironmaking & Steelmaking
Processes, Products and Applications
Volume 46, 2019 - Issue 7
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Research Articles

Fuel enhancement by conversion of hotter waste CO2 in flue gas with coke

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Pages 632-640 | Received 15 Dec 2017, Accepted 29 Jan 2018, Published online: 21 Feb 2018
 

ABSTRACT

Considering the huge losses of high-temperature metallurgical waste heat and gases in steel works and the energy crisis on a worldwide scale, particularly the waste hotter gases in the flue of a converter that are emitted into air, a novel concept where coke is injected into the hotter gases for enhancement of fuel gas and reduction of CO2 emissions into air is proposed. The effect of the surface structure of coke on the reactions of gas–solid phases was analysed using the t-plot method, and the transient gas products were described during coke injection. The energy change of the flue gas under various injecting schemes was discussed during the tests. The results show that an injecting scheme comprising an injecting pressure of 1.0 MPa, an inserted depth of 500 mm and an injecting mass rate of 18 kg min−1 seems to be better. The value of the specific surface area of coke was 8.36 m2 g−1, while the coal was 20.59 m2 g−1. With the inserted depth at 400 and 500 mm, the recovery time of the flue gas was 545 and 565 s and the total calorific value accounted for 48.47 and 51.53%, respectively. Without injection, the average contents of CO, O2 and CO2 were 48.1, 1.01 and 23.3, whereas after injection the average contents of CO, O2 and CO2 were 56, 0.5 and 10.1%, respectively. As a result, this process reduces CO2 emissions and increases energy of the flue gas.

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Correction

Acknowledgements

The authors sincerely thank Prof. Zhou Jian-an (working in Wuhan University of Science and Technology) for giving great help in data acquisition of industrial test. This work sincerely thanks Prof. Zhang Hua and colleague engineer Jiang Xue-kai because they participated in the industrial pilot tests. This work sincerely thanks the E-chen Iron & Steel Corp. E-zhou City Hubei Province, China, because this steel plant provided the industrial pilot tests in 30 ton steelmaking converter. The test time lasted nearly eight months. This paper also sincerely thanks all the participants who offered help and made great contributions to this work.

Disclosure statement

No potential conflict of interest was reported by the authors.

Correction Statement

This article was originally published with errors, which have now been corrected in the online version. Please see Correction (http://dx.doi.org/10.1080/03019233.2022.2109114)

Additional information

Funding

This research was supported by Wuhan Iron and Steel Group Echen Iron and Steel Co., Ltd, Hubei province, China.

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